Muddy Toes
12-01-2012, 12:03 AM
Alright here I go, never done a report before but under instruction from Marty Seaweed I shall begin my first.Lets hope future ones will be less dramatic.:o
Left Victoria Point boat ramp at 0400 this morning to be met by a glassed out bay.Opened up my brand new 300 yammie which saw us crossing the bar not long after sunrise.Conditions were great as we sounded out some ground on the 29's and 33's, tiny swell and hardly a breath of wind and current pulling about half a knot.It seemed like it was going to be the perfect day.Found the fish on the 33's after a bit of sounding around so it was time to set up for a drift and deploy some baits, life couldn't get any better, the weather was awesome.
About half way through our first drift the bilge pump spurts out a bit of water and I think nothing much of it.Another couple of minutes later it does the same thing.I'm now at the stage that I'm starting to think something may be wrong so my mate and I put our rods down and lift up the inspection hatch at the stern to find an alarming amount of water filling up the bilge and every time we scrambled around the boat to try and figure out what was happening more water would gush in as the boat rocked.By this time the bilge pump is working it's tits off with a solid flow of water coming out of the bilge but it seemed like it was fighting a losing battle....the pump could never have kept up.:oIn about two seconds flat the lines were in, rods stowed and we were heading towards Moreton at about well ummm a 300hp at WOT speed with life jackets on, grab bag in hand and on the look out for other boats.Whilst I was driving I had my mate stay down the back and let me know what the water level in the bilge was doing.After a while the water level in the bilge started to drop and after about 10 minutes the bilge pump had won it's little fight and had it under control.By this stage I was starting to think maybe the hull had been breached in the bow somewhere and while it was on the plane with the nose in the air no water was getting in.So after what seemed to be the longest ride of my life we were back through the bar down the bay and back at Victoria Point with an empty bilge.Tied up to the pontoon we removed the inspection hatch and waited to see if the bilge would once again fill up whist at rest but it didn't.By then we started to check all the hoses, fitting and pumps in the hull only to find the hose that drains my live bait tank via a seacock at the waterline was disconnected.It all started to make sense now, at rest offshore with a little bit of swell and the boat moving slightly water was being forced in to the seacock and in to the bilge and on the plane it was fine as the water was just rushing past the seacock and not being forced in to it.A while later the hose was back on and the hose clamps tightened and the rest of the fittings checked.
At the time it seemed apparent that in order to remove my old motors cables and run my new ones the dealer removed the hose and forgot to put it back on.I rung the dealership i bought my motor off to let them know what had happened only to be told that it was very unlikely that it would have been disconnected during the installation.They said it may have been pulled off by accident whilst running my new cables but they remained adamant it was not their fault.Not that i really care now but it was obviously not clamped on properly in the first place when it was done in September last year and the dealer pulled it off accidently when running the new cables or the dealer took it off and forgot to put it back on......you decide, I'm over it.
By now it's mid morning and despite mixed weather reports we ballsed up and headed back out and do it all over again.Back out to the 33's and the weather is still great, actually my only gripe was that there wasn't enough wind to give some relief from the heat of the day....it was that good.We tried a few different baits but it was squid on a floater that did the damage on the squire.After a few drifts the fish started to shut down so we decided to use these good conditions to do a bit of sounding around to find some new ground for a later date.We came across a little patch of reef near square patch and floated some baits down to find a good size cod.About 1400 the wind started to pick up a bit and we decided to call it a day with a few fish and the boat still floating.:-[
Amen.
Stats on the trip......
250km traveled
210ltrs fuel used
1kg squid
1kg pillies
1 pizza
6 cans of coke
pack of durries
756927569375694
Left Victoria Point boat ramp at 0400 this morning to be met by a glassed out bay.Opened up my brand new 300 yammie which saw us crossing the bar not long after sunrise.Conditions were great as we sounded out some ground on the 29's and 33's, tiny swell and hardly a breath of wind and current pulling about half a knot.It seemed like it was going to be the perfect day.Found the fish on the 33's after a bit of sounding around so it was time to set up for a drift and deploy some baits, life couldn't get any better, the weather was awesome.
About half way through our first drift the bilge pump spurts out a bit of water and I think nothing much of it.Another couple of minutes later it does the same thing.I'm now at the stage that I'm starting to think something may be wrong so my mate and I put our rods down and lift up the inspection hatch at the stern to find an alarming amount of water filling up the bilge and every time we scrambled around the boat to try and figure out what was happening more water would gush in as the boat rocked.By this time the bilge pump is working it's tits off with a solid flow of water coming out of the bilge but it seemed like it was fighting a losing battle....the pump could never have kept up.:oIn about two seconds flat the lines were in, rods stowed and we were heading towards Moreton at about well ummm a 300hp at WOT speed with life jackets on, grab bag in hand and on the look out for other boats.Whilst I was driving I had my mate stay down the back and let me know what the water level in the bilge was doing.After a while the water level in the bilge started to drop and after about 10 minutes the bilge pump had won it's little fight and had it under control.By this stage I was starting to think maybe the hull had been breached in the bow somewhere and while it was on the plane with the nose in the air no water was getting in.So after what seemed to be the longest ride of my life we were back through the bar down the bay and back at Victoria Point with an empty bilge.Tied up to the pontoon we removed the inspection hatch and waited to see if the bilge would once again fill up whist at rest but it didn't.By then we started to check all the hoses, fitting and pumps in the hull only to find the hose that drains my live bait tank via a seacock at the waterline was disconnected.It all started to make sense now, at rest offshore with a little bit of swell and the boat moving slightly water was being forced in to the seacock and in to the bilge and on the plane it was fine as the water was just rushing past the seacock and not being forced in to it.A while later the hose was back on and the hose clamps tightened and the rest of the fittings checked.
At the time it seemed apparent that in order to remove my old motors cables and run my new ones the dealer removed the hose and forgot to put it back on.I rung the dealership i bought my motor off to let them know what had happened only to be told that it was very unlikely that it would have been disconnected during the installation.They said it may have been pulled off by accident whilst running my new cables but they remained adamant it was not their fault.Not that i really care now but it was obviously not clamped on properly in the first place when it was done in September last year and the dealer pulled it off accidently when running the new cables or the dealer took it off and forgot to put it back on......you decide, I'm over it.
By now it's mid morning and despite mixed weather reports we ballsed up and headed back out and do it all over again.Back out to the 33's and the weather is still great, actually my only gripe was that there wasn't enough wind to give some relief from the heat of the day....it was that good.We tried a few different baits but it was squid on a floater that did the damage on the squire.After a few drifts the fish started to shut down so we decided to use these good conditions to do a bit of sounding around to find some new ground for a later date.We came across a little patch of reef near square patch and floated some baits down to find a good size cod.About 1400 the wind started to pick up a bit and we decided to call it a day with a few fish and the boat still floating.:-[
Amen.
Stats on the trip......
250km traveled
210ltrs fuel used
1kg squid
1kg pillies
1 pizza
6 cans of coke
pack of durries
756927569375694