NormC
24-11-2008, 08:07 PM
It has taken a while, but I finally got my new tinnie on the water today for it's first run. Some issues to sort out, but perhaps not as bad as I first thought.
This is a tinnie I have set up for roof topping when we travel. It is my third and biggest 'roof topper'. I certainly can't see myself going any bigger!
It is a Sea Jay Angler 3.95, powered by a Mercury 30 HP 4 Stroke electric start, gas assisted tilt. Also fitted with 55 lb Minn Kota, home made live bait tank, and lots of other creature comforts like padded seats, removable carpeted floor, casting platform / storage area in front of front thwart, rod holders (5) rod storage (for 5 rods), glove box etc.
I bought the hull from Satisfaction Marine on the Gold Coast. I organised to pick the boat up from the Sea Jay factory in Bundaberg as I was getting a boat loader / rack built by another company in Bundaberg. I dropped into Satisfaction Marine a couple of weeks ago and paid the balance for the boat and rego. The boat was picked up in Bundaberg a few days later. The next day, Satisfaction Marine closed down and is in receivership. Lucky me. If the boat was collected from Sea Jay a day or two later, I might never have got it and would have lost my money (assuming Satisfaction had not yet paid Sea Jay). But not all good news. Although I paid Satisfaction to register the boat, they had not completed the process. After several days and a few phone calls, it became clear I would have to do this myself and pay a second time. I did this today at the local Queensland Transport office.
While waiting to sort out the rego, I did all the mods mentioned in the first para. So with boat finally set up and registered, I hit the water in the Coomera River for the first time this afternoon.
Not a happy experience. Despite the 30 HP motor on a 3.95 boat, I could not get on the plane. The motor weighs 72 KG. Plus I had a full fuel tank (25KG) and a 100AH AGM battery (36KG), the bait tank and a few other things behind the rear thwart (offset to some extent by Minn Kota up front). I moved the fuel tank forward and with a lot of effort got on the plane, but now experienced lots of porpoising. Not good.
I returned to the boat ramp to check that the trim pin was in the bottom position. It was. I then noticed a lot of water in the boat. This is not looking like the great afternoon I was planning on.
Packed up and headed home. I stripped everything out from behind the rear thwart. Firstly to reduce weight, second to check where the leak might be (I had penetrated the hull a few times during the boat set up (bolting motor on, fitting transducer bracket, fitting bracket for bilge pump for bait tank).
With the stripped down version, I headed back to the river. After launching, when I lowered the motor, I learnt on it and noticed it dropped a bit further. Mmmm, looks like the gas assist has enough pressure (when new at least) to hold the motor up a fraction against it's own weight. I left the fuel tank forward for the first run. Rope start needed as I had removed the battery. Popped up on the plane in about half a second when I hit the throttle. Moved the fuel tank to behind the rear thwart. Same thing - on the plane in an instant. Check for leaks. A small dribble from one of my penetrations that I did not seal well enough, but nothing serious.
Went for a run for 90 mins for run in and about 2 liters of water in the boat. All performing well. Being a run in, no WOT yet, but looks like it will fly.
Headed home. Resealed the leak. Refitted all the 'stuff' I had removed but by now it was almost 6.00PM. Will hit the water again tomorrow to see if the initial problem was motor not dropping fully down (ie inadvertently running with the motor trimmed up a bit first time). Hopefully that is the issue. If not, I have some rework to do. First step I suspect is to move the battery forward.
Although the 4 Stroke lacks the torque of a two stroke, the only additional weight on the back of this boat compared to my last one is the 25 KG of extra motor weight (previous was 20 HP 2 stroke). I will certainly be disappointed if after ensuring the motor is fully lowered, I don't pop up on the plane instantly.
Hopefully I'll post a happy follow up tomorrow.
Norm C
This is a tinnie I have set up for roof topping when we travel. It is my third and biggest 'roof topper'. I certainly can't see myself going any bigger!
It is a Sea Jay Angler 3.95, powered by a Mercury 30 HP 4 Stroke electric start, gas assisted tilt. Also fitted with 55 lb Minn Kota, home made live bait tank, and lots of other creature comforts like padded seats, removable carpeted floor, casting platform / storage area in front of front thwart, rod holders (5) rod storage (for 5 rods), glove box etc.
I bought the hull from Satisfaction Marine on the Gold Coast. I organised to pick the boat up from the Sea Jay factory in Bundaberg as I was getting a boat loader / rack built by another company in Bundaberg. I dropped into Satisfaction Marine a couple of weeks ago and paid the balance for the boat and rego. The boat was picked up in Bundaberg a few days later. The next day, Satisfaction Marine closed down and is in receivership. Lucky me. If the boat was collected from Sea Jay a day or two later, I might never have got it and would have lost my money (assuming Satisfaction had not yet paid Sea Jay). But not all good news. Although I paid Satisfaction to register the boat, they had not completed the process. After several days and a few phone calls, it became clear I would have to do this myself and pay a second time. I did this today at the local Queensland Transport office.
While waiting to sort out the rego, I did all the mods mentioned in the first para. So with boat finally set up and registered, I hit the water in the Coomera River for the first time this afternoon.
Not a happy experience. Despite the 30 HP motor on a 3.95 boat, I could not get on the plane. The motor weighs 72 KG. Plus I had a full fuel tank (25KG) and a 100AH AGM battery (36KG), the bait tank and a few other things behind the rear thwart (offset to some extent by Minn Kota up front). I moved the fuel tank forward and with a lot of effort got on the plane, but now experienced lots of porpoising. Not good.
I returned to the boat ramp to check that the trim pin was in the bottom position. It was. I then noticed a lot of water in the boat. This is not looking like the great afternoon I was planning on.
Packed up and headed home. I stripped everything out from behind the rear thwart. Firstly to reduce weight, second to check where the leak might be (I had penetrated the hull a few times during the boat set up (bolting motor on, fitting transducer bracket, fitting bracket for bilge pump for bait tank).
With the stripped down version, I headed back to the river. After launching, when I lowered the motor, I learnt on it and noticed it dropped a bit further. Mmmm, looks like the gas assist has enough pressure (when new at least) to hold the motor up a fraction against it's own weight. I left the fuel tank forward for the first run. Rope start needed as I had removed the battery. Popped up on the plane in about half a second when I hit the throttle. Moved the fuel tank to behind the rear thwart. Same thing - on the plane in an instant. Check for leaks. A small dribble from one of my penetrations that I did not seal well enough, but nothing serious.
Went for a run for 90 mins for run in and about 2 liters of water in the boat. All performing well. Being a run in, no WOT yet, but looks like it will fly.
Headed home. Resealed the leak. Refitted all the 'stuff' I had removed but by now it was almost 6.00PM. Will hit the water again tomorrow to see if the initial problem was motor not dropping fully down (ie inadvertently running with the motor trimmed up a bit first time). Hopefully that is the issue. If not, I have some rework to do. First step I suspect is to move the battery forward.
Although the 4 Stroke lacks the torque of a two stroke, the only additional weight on the back of this boat compared to my last one is the 25 KG of extra motor weight (previous was 20 HP 2 stroke). I will certainly be disappointed if after ensuring the motor is fully lowered, I don't pop up on the plane instantly.
Hopefully I'll post a happy follow up tomorrow.
Norm C